Skip to content
New issue

Have a question about this project? Sign up for a free GitHub account to open an issue and contact its maintainers and the community.

By clicking “Sign up for GitHub”, you agree to our terms of service and privacy statement. We’ll occasionally send you account related emails.

Already on GitHub? Sign in to your account

Jkbms_Can: Cell count: 1 | Cells populated: 0 && TypeError: '>' not supported between instances of 'float' and 'NoneType' #950

Closed
p0l0us opened this issue Feb 4, 2024 · 3 comments
Labels
bug Something isn't working

Comments

@p0l0us
Copy link
Contributor

p0l0us commented Feb 4, 2024

Describe the bug

Hi, I'm trying to run my Jk bms over CAN bus using this project. When I setup everything and make running, the bms entry is appearing and disappearing from the VenusOS screen - most likely the driver is constantly restarting or so. When it is visible, no data shown (all fields empty).

image

image

See logs bellow for details. It looks like there is Cells populated: 0 which leads to TypeError: '>' not supported between instances of 'float' and 'NoneType'. Can anyone give me any ideas ?

Similar problem with zero cells I noticed with Daly_Can.

I tested with master (commit e3206f7) and dev (commit 5e025e6). Project didn't run with latest release since I had a python wheels issue.

Hardware: RaspberryPI zero 2w with clean VenusOS 3.14 large image, CAN Bus adapter MCP2515/TJA1050, JK BMS B2A8S20P heat can.

CAN adapter is connected according to: https://forums.raspberrypi.com/viewtopic.php?t=141052, with dtoverlay=mcp2515-can0,oscillator=8000000,interrupt=12 in boot config.txt. I confirmed that my can0 works against computer at 250kbps. I see "some" can messages from the JK bms on the computer as well in the canable cangaroo app (all are on the same can bus).

image

candump can0

  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  4F5   [8]  DD 0C 01 DC 0C 02 55 AA
  can0  5F5   [8]  3A 01 3A 00 11 55 00 AA
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  4F5   [8]  DC 0C 01 DC 0C 02 55 AA
  can0  5F5   [8]  3A 01 3A 00 11 55 00 AA
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  4F5   [8]  DC 0C 01 DD 0C 02 55 AA
  can0  5F5   [8]  3A 01 3A 00 11 55 00 AA
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  4F5   [8]  DC 0C 01 DD 0C 02 55 AA
  can0  5F5   [8]  3A 01 3A 00 11 55 00 AA
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  4F5   [8]  DC 0C 01 DD 0C 02 55 AA
  can0  5F5   [8]  3A 01 3A 00 11 55 00 AA
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01
  can0  4F5   [8]  DC 0C 01 DD 0C 02 55 AA
  can0  5F5   [8]  3A 01 3A 00 11 55 00 AA
  can0  2F5   [8]  83 00 9F 0F 04 AA 4A 01

How to reproduce

  1. Installed clean venus os on my rpi zero 2w, connected to wifi, made ssh
  2. connected CAN adaper, set CAN speed to 250kbps
  3. tested CAN with PC (both, JK bms and rpi with venus)
  4. installed dbus_serialbattery according to documentation (dev and master)
  5. enabled DVCC
  6. set the config.ini
  7. reinstall dbus_serialbattery & reboot

Expected behavior

I see the Jk bms entry on the venusos board.

Driver version

e3206f7

Venus OS device type

Raspberry Pi 2

Venus OS version

3.14

BMS type

Daly Smart BMS, JKBMS / Heltec BMS

Cell count

4

Battery count

1

Connection type

Serial USB adapter to TTL

Config file

[DEFAULT]
LOGGING = DEBUG
CAN_PORT = can0
BMS_TYPE = Jkbms, Jkbms_Can

Relevant log output

2024-02-04 12:58:53.026649500 INFO:SerialBattery:
2024-02-04 12:58:53.027291500 INFO:SerialBattery:Starting dbus-serialbattery
2024-02-04 12:58:53.028287500 INFO:SerialBattery:dbus-serialbattery v1.0.20231117dev
2024-02-04 12:58:53.766530500 INFO:SerialBattery:-- Testing BMS: 1 of 3 rounds
2024-02-04 12:58:53.767151500 INFO:SerialBattery:Testing Jkbms_Can
2024-02-04 12:58:53.768072500 DEBUG:SerialBattery:Can bus init
2024-02-04 12:58:53.842501500 DEBUG:SerialBattery:Can bus init done
2024-02-04 12:58:55.192490500 INFO:SerialBattery:Connection established to Jkbms_Can
2024-02-04 12:58:55.193168500 INFO:SerialBattery:Battery Jkbms_Can connected to dbus from can0
2024-02-04 12:58:55.193757500 INFO:SerialBattery:========== Settings ==========
2024-02-04 12:58:55.194309500 INFO:SerialBattery:> Connection voltage: NoneV | Current: NoneA | SoC: None%
2024-02-04 12:58:55.194822500 INFO:SerialBattery:> Cell count: 1 | Cells populated: 0
2024-02-04 12:58:55.195345500 INFO:SerialBattery:> LINEAR LIMITATION ENABLE: True
2024-02-04 12:58:55.195894500 INFO:SerialBattery:> MAX BATTERY CHARGE CURRENT: 50.0A | MAX BATTERY DISCHARGE CURRENT:                                                                                                                         60.0A
2024-02-04 12:58:55.196417500 INFO:SerialBattery:> CVCM:     True
2024-02-04 12:58:55.196960500 INFO:SerialBattery:> MIN CELL VOLTAGE: 2.9V | MAX CELL VOLTAGE: 3.45V
2024-02-04 12:58:55.197496500 INFO:SerialBattery:> CCCM CV:  True  | DCCM CV:  True
2024-02-04 12:58:55.198020500 INFO:SerialBattery:> CCCM T:   True  | DCCM T:   True
2024-02-04 12:58:55.198544500 INFO:SerialBattery:> CCCM SOC: True  | DCCM SOC: True
2024-02-04 12:58:55.199069500 INFO:SerialBattery:Serial Number/Unique Identifier: NoneAh
2024-02-04 12:58:55.235715500 INFO:SerialBattery:DeviceInstance = 4
2024-02-04 12:58:55.236534500 INFO:SerialBattery:com.victronenergy.battery.can0
2024-02-04 12:58:55.257097500 INFO:SerialBattery:publish config values = 1
2024-02-04 12:58:56.820386500 Traceback (most recent call last):
2024-02-04 12:58:56.820393500   File "/opt/victronenergy/dbus-serialbattery/dbushelper.py", line 389, in publish_batt                                                                                                                        ery
2024-02-04 12:58:56.820398500     self.battery.manage_charge_current()
2024-02-04 12:58:56.820401500   File "/opt/victronenergy/dbus-serialbattery/battery.py", line 580, in manage_charge_c                                                                                                                        urrent
2024-02-04 12:58:56.820406500     if utils.MAX_BATTERY_CHARGE_CURRENT > self.max_battery_charge_current:
2024-02-04 12:58:56.820410500 TypeError: '>' not supported between instances of 'float' and 'NoneType'
2024-02-04 12:58:57.037272500
2024-02-04 12:58:58.125645500 INFO:SerialBattery:
2024-02-04 12:58:58.126370500 INFO:SerialBattery:Starting dbus-serialbattery
2024-02-04 12:58:58.127602500 INFO:SerialBattery:dbus-serialbattery v1.0.20231117dev

Any other information that may be helpful

No response

@p0l0us p0l0us added the bug Something isn't working label Feb 4, 2024
@p0l0us
Copy link
Contributor Author

p0l0us commented Feb 4, 2024

After changing CAN_FRAMES in the jkbms_can.py to following, some BMS data was read correctly:

Connection voltage: 13.1V | Current: -4.5A | SoC: 4%

but cell count 3 still doesn't seem to be correct and I'm still facing the TypeError

    CAN_FRAMES = {
        BATT_STAT: 0x02F5,
        CELL_VOLT: 0x04F5,
        CELL_TEMP: 0x05F5,
        ALM_INFO: 0x07F5,
    }
2024-02-04 15:32:55.582081500 INFO:SerialBattery:
2024-02-04 15:32:55.582713500 INFO:SerialBattery:Starting dbus-serialbattery
2024-02-04 15:32:55.583704500 INFO:SerialBattery:dbus-serialbattery v1.0.20231117dev
2024-02-04 15:32:56.323313500 INFO:SerialBattery:-- Testing BMS: 1 of 3 rounds
2024-02-04 15:32:56.323938500 INFO:SerialBattery:Testing Jkbms_Can
2024-02-04 15:32:56.324844500 DEBUG:SerialBattery:Can bus init
2024-02-04 15:32:56.399649500 DEBUG:SerialBattery:Can bus init done
2024-02-04 15:32:57.748679500 INFO:SerialBattery:Connection established to Jkbms_Can
2024-02-04 15:32:57.749491500 INFO:SerialBattery:Battery Jkbms_Can connected to dbus from can0
2024-02-04 15:32:57.750182500 INFO:SerialBattery:========== Settings ==========
2024-02-04 15:32:57.750917500 INFO:SerialBattery:> Connection voltage: 13.1V | Current: -4.5A | SoC: 4%
2024-02-04 15:32:57.751556500 INFO:SerialBattery:> Cell count: 3 | Cells populated: 3
2024-02-04 15:32:57.752282500 INFO:SerialBattery:> LINEAR LIMITATION ENABLE: True
2024-02-04 15:32:57.752952500 INFO:SerialBattery:> MAX BATTERY CHARGE CURRENT: 50.0A | MAX BATTERY DISCHARGE CURRENT: 60.0A
2024-02-04 15:32:57.753781500 INFO:SerialBattery:> CVCM:     True
2024-02-04 15:32:57.754468500 INFO:SerialBattery:> MIN CELL VOLTAGE: 2.9V | MAX CELL VOLTAGE: 3.45V
2024-02-04 15:32:57.755121500 INFO:SerialBattery:> CCCM CV:  True  | DCCM CV:  True
2024-02-04 15:32:57.755853500 INFO:SerialBattery:> CCCM T:   True  | DCCM T:   True
2024-02-04 15:32:57.756706500 INFO:SerialBattery:> CCCM SOC: True  | DCCM SOC: True
2024-02-04 15:32:57.757466500 INFO:SerialBattery:Serial Number/Unique Identifier: JKBMSCAN3cells_NoneAh
2024-02-04 15:32:57.811788500 INFO:SerialBattery:DeviceInstance = 4
2024-02-04 15:32:57.812386500 INFO:SerialBattery:com.victronenergy.battery.can0
2024-02-04 15:32:57.834986500 INFO:SerialBattery:publish config values = 1
2024-02-04 15:32:59.406252500 Traceback (most recent call last):
2024-02-04 15:32:59.406258500   File "/opt/victronenergy/dbus-serialbattery/dbushelper.py", line 389, in publish_battery
2024-02-04 15:32:59.406263500     self.battery.manage_charge_current()
2024-02-04 15:32:59.406266500   File "/opt/victronenergy/dbus-serialbattery/battery.py", line 580, in manage_charge_current
2024-02-04 15:32:59.406271500     if utils.MAX_BATTERY_CHARGE_CURRENT > self.max_battery_charge_current:
2024-02-04 15:32:59.406275500 TypeError: '>' not supported between instances of 'float' and 'NoneType'
2024-02-04 15:32:59.630628500
2024-02-04 15:33:00.765353500 INFO:SerialBattery:
2024-02-04 15:33:00.766070500 INFO:SerialBattery:Starting dbus-serialbattery
2024-02-04 15:33:00.767314500 INFO:SerialBattery:dbus-serialbattery v1.0.20231117dev
2024-02-04 15:33:01.537696500 INFO:SerialBattery:-- Testing BMS: 1 of 3 rounds
2024-02-04 15:33:01.538409500 INFO:SerialBattery:Testing Jkbms_Can
2024-02-04 15:33:01.539847500 DEBUG:SerialBattery:Can bus init
2024-02-04 15:33:01.616658500 DEBUG:SerialBattery:Can bus init done

@p0l0us
Copy link
Contributor Author

p0l0us commented Feb 4, 2024

It seems exception and rest of troubles are fixed by following:

jkbms_can.py

self.max_battery_current = MAX_BATTERY_CHARGE_CURRENT

change to

self.max_battery_charge_current = MAX_BATTERY_CHARGE_CURRENT

Same self.max_battery_charge_current issue seems to be in daly_can.py

p0l0us added a commit to p0l0us/dbus-serialbattery that referenced this issue Feb 4, 2024
p0l0us added a commit to p0l0us/dbus-serialbattery that referenced this issue Feb 4, 2024
p0l0us added a commit to p0l0us/dbus-serialbattery that referenced this issue Feb 4, 2024
@p0l0us p0l0us mentioned this issue Feb 4, 2024
p0l0us added a commit to p0l0us/dbus-serialbattery that referenced this issue Feb 9, 2024
Fixing Louisvdw#950 for DalyBMS
p0l0us added a commit to p0l0us/dbus-serialbattery that referenced this issue Feb 9, 2024
@p0l0us p0l0us mentioned this issue Feb 9, 2024
mr-manuel pushed a commit to mr-manuel/venus-os_dbus-serialbattery that referenced this issue Feb 11, 2024
mr-manuel pushed a commit to mr-manuel/venus-os_dbus-serialbattery that referenced this issue Feb 11, 2024
Louisvdw pushed a commit that referenced this issue Feb 28, 2024
* fix Sinowealth not loading
#702

* fix unique identifier function

* enable BMS over config, if disabled by default
Now you can also add more then one BMS for BMS_TYPE

* show battery port in log

* ANT BMS fixes
Fixed that other devices are recognized as ANT BMS

* Sinowealth BMS fixes
Fixed that other devices are recognized as Sinowealth BMS

* improved publish_battery error handling
switched from error count to seconds

* Improve Battery Voltage Handling in Linear Absorption Mode

* Refactor change time() to int(time()) for consistency in max_voltage_start_time and tDiff calculation
* Refactor battery voltage calculations for efficiency and clarity
* Remove penalty_buffer
* Reset max_voltage_start_time wenn we going to bulk(dynamic) mode

* updated changelog

* fix reply processing

* Reduce the big inrush current, if the CVL jumps
from Bulk/Absorbtion to Float
fix #659

* Check returned data lenght for Seplos BMS

Be stricter about the return data we accept, might fix the problem of grid meters accidently being recognized as a Seplos

* Validate current, voltage, capacity and SoC for all BMS
This prevents that a device, which is no BMS, is detected as BMS

* removed double check

* bump version

* fix validation if None

* updated changelog

* proposal to #659 formatted :)

* bugfix proposal to #659

* refactor setting float charge_mode

* fix type error, removed bluetooth cronjob

* updated changelog

* fix rs485 write communication errors by inserting sleeps, add debug print for charge mode and fix crash on write soc failures

* fix write problem on set_soc. also changed the switch charge/discharge function, just in case

* debug msg

* Bluetooth optimizations

* Fixes by @peterohman
#505 (comment)

* fix #712

* fix meaningless time to go values

* fix meaningless time to go values

* Duration of transition to float depends on number of cells

* Float transition - Voltage drop per second

* Update hlpdatabms4s.py

* Validate setting of FLOAT_CELL_VOLTAGE and avoid misconfiguration

* consider utils.LINEAR_RECALCULATION_EVERY to refresh CVL

* cleanup

* consider utils.LINEAR_RECALCULATION_EVERY to refresh CVL

* small refactor, introduced set_cvl_linear function to set CVL only once every LINEAR_RECALCULATION_EVERY seconds

* fix typo

* updated changelog

* remove debug msg

* remove debug msg

* undo debug change

* Daly BMS make auto reset soc configurable

* added debug and error information for CVL

* fix proposal for #733 (#735)

* Added: Tollerance to enter float voltage once the timer is triggered

* Add bulk voltage
Load to bulk voltage every x days to reset the SoC to 100% for some BMS

* JKBMS disable high voltage warning on bulk
reenable after bulk was completed

* fixed error

* disable high voltage warning for all BMS
when charging to bulk voltage

* fix error and change default value
measurementToleranceVariation from 0.025 to 0.5 else in OffGrid mode max voltage is always kept

* Added temperature names to dbus/mqtt

* Use current avg of last 300 cycles for TTG & TTS

* Calculate only positive Time-to-SoC points

* added current average of last 5 minutes

* make CCL and DCL more clear

* fix small error

* bugfix: LLTJBD BMS SOC different in Xiaoxiang app and dbus-serialbattery

* black formatting

* JDB BMS - Control FETs for charge, discharge and disable / enable balancer (#761)

* feature: Allow to control charge / discharge FET
* feature: Allow to enable / disable balancer

* bugfix: Cycle Capacity is in 10 mAh

Fixes SoC with factor 100 * 100% percentage

* JBD BMS show balancer state in GUI page IO (#763)

* Bump version

* Fix typos

* Smaller fixes
- fixes #792 (comment)

* Removed comments from utils.py
This should make more clear that there are no values to change

* Updated changelog

* possible fix for LLT/JBS connection problems
#769
#777

* bugfix: LLT/JBD BMS general packet data size check

* improved reinstall and disable script

* LLT/JBD BMS - Improved error handling and automatical driver restart
in case of error. Should fix:
- #730
- #769
- #777

* Fixed Building wheel for dbus-fast won't finish on weak systems
Fixes #785

* Support for Daly CAN Bus (#169)

* support for Daly CAN Bus
* fix constructor args
* revert port, needs fix
* add can filters
* comment logger

Some changes are still needed to work with the latest version. They will follow in a next PR.

---------

Co-authored-by: Samuel Brucksch <[email protected]>
Co-authored-by: Manuel <[email protected]>

* JKBMS BLE - Introduction of automatic SOC reset (HW Version 11) (#736)

* Introduction of automatic SOC reset for JK BMS (HW Version 11)
* Fixed value mapping
* Rework of the code to make it simpler to use without additional configuration.
Moved execution of SOC reset. It's now executed while changing from "Float" to "Float Transition".
* Implementation of suggested changes
Persist initial BMS OVP and OVPR settings
Make use of max_cell_voltage to calculate trigger value for OVP alert

* Added: Daly CAN and JKBMS CAN

* added CAN bms to installation script
optimized CAN drivers

* smaller fixes

* Trigger JK BLE SOC reset when using Step Mode

* Moved trigger_soc_reset()

* fixes LLT/JBD SOC > 100%
#769

* changed VOLTAGE_DROP behaviour

* Fix JKBMS not starting if BMS manuf. date is empty

* corrected bulk, absorption and soc reset terms

* fix typo

* add JKBMS_BLE debugging data

* fix small error

* Some changes for lost bluetooth connection / hci_uart stack restart

* added logging to config

* add sleep before starting driver
prevents lot of timeouts after reinstalling the driver, since the restart is now much faster than before

* changed post install info

* fix error

* Daly BMS fixed embedded null byte
#837

* added info for SoC reset to default config file

* fix for #716
#716

* fix for #716 and JKBMS model recognition
#716

* optimized logging

* fix JKBMS recognition

* added debugging

* fixes #716
#716

* Bind device instance to unique_identifier
#718

* added data types to battery class
disabled unused variables

* save current charge state
#840

* correct file permissions

* updated changelog

* added periodic saveChargeDetails

* fix some small errors

* fix issue with ruuvi tags
When there are hundreds of unused ruuvi tags in the settings list that where added because thei where nearby the driver does not start correctly. These stale entries are disabled on the driver startup.
The issue was already filed to Victron developers

* CVL with i-controller instead of penaltysum

* cvl_controller: switch to choose PenaltySum or ICOntroller + documentation

* docu enhancement

* Add setting and install logic for usb bluetooth module

* round temperatures

* changed battery disconnect behaviour

* Fixes #891
#891

* updated changelog

* Add bluetooth device note to config.default.ini

* Fix typo in bluetooth note in config.default.ini

* fixed error in new cvl_controller

* fixed float division by zero and code optimization

* Restart MAX_VOLTAGE_TIME_SEC if cell diff > CELL_VOLTAGE_DIFF_KEEP_MAX_VOLTAGE_TIME_RESTART

* Calculation of the SOC based on coloumb-counting (#868)

* Calculation of the SOC in the driver based on coloumb-counting

* soc_calc: add current correction before integration

* soc_calc: correction map for current

* Soc_calc: CorrectionMap, switch to turn on/off correction, selectable initial value

* soc_calc: Bugfix

* soc_calc: Bugfix

* store soc in dbus for restart

* store soc in dbus for restart (formatted)

* store soc in dbus for restart (bugfix)

* save soc_calc only after change > 1.0

* store soc in dbus for restart (bugfix)

* logger does not work this way. do not know why

* writing and reading to dbus works

* Removed options: SOC_CALC_CURRENT_CORRECTION, SOC_CALC_RESET_VALUE_ON_RESTART, SOC_CALC_INIT_VALUE
sort soc_calc alphabetically

* fixed comments

* Updated changelog, small fixes

* Changed: PUBLISH_CONFIG_VALUES from 0/1 to True/False

* Changed: Code optimizations
- Changed some variables to be more clear
- Added comments for easier code understanding

* Calculated SOC: Added two decimals, added BMS SOC for MQTT & Node-RED

* Updated changelog, small fixes

* Changed: PUBLISH_CONFIG_VALUES from 0/1 to True/False

* Changed: Code optimizations
- Changed some variables to be more clear
- Added comments for easier code understanding

* Calculated SOC: Added two decimals, added BMS SOC for MQTT & Node-RED

* Fix #898
#898

* Changed: Fix issue loading settings from dbus

* Added nightly install option
makes it easier for users to pretest fixes

* Changed: more detailed error output when an exception happens

* Possible fix for #912
#912

* Fixes #919
#919

* Changed: Exit script with error, if port excluded
else the serialstarter stops at the dbus-serialbattery

* Fixed some smaller errors

* Updated pre-release workflow

* Fix JK BMS connection restart when bluetooth fails.

This fix installs a new thread to monitor the state of the original
scraping thread.
If scraping thread dies, it verifies that it did not because the
scraping was intentionally stopped by calling stop_scrapping.
When restarting the scrapper, it first calls the bluetooth
reset lambda function that was passed in the class contructor, such that
bluetooth is ready to make a proper connection.

* Fixes #916
#916

* Added Venus OS version to logfile

* Fix #840
#840

* Small code formatting fixes

* Optimized reinstall script. Restart GUI only on changes.

* Display debugging data in GUI when DEBUG enabled

* Install script now shows repositories and version numbers

* Update daly_can.py

Fixing #950 for DalyBMS

* Update jkbms_can.py

Fixing #950 for Jk BMS

* Fix black lint check

* Fixes #970
#970

* Fixed some errors in restoring values from dbus settings

* Moved sleep on start for all BMS

* Update config description

* Reworked a part of the default config

* fix typo in stopping services when reinstalling

* Fix Time-to-SoC and Time-to-Go calculation

* Add changelog info

* Round sum and diff voltage

* Temperature limitation variables where changed

* SoC limitation variables where changed

* Added error messages

* Remove unneeded code

* Reset SoC to 0% if empty

* Add GUIv2 for dbus-serialbattery

* Check free space before installing

* Added new GUIv2 version

* Removed Python 2 compatibility

* Changelog update

* Code cleanup
- Removed: get_temperatures()
- Removed: update_last_seen()

* Bluetooth code optimizations

* Fixed some JKBMS BLE not starting
#819

* Check if packages are already installed before install

* Fixed some SOC calculation errors

* Fixed None SOC on driver start

* Do not show and allow button change when callback is missing for:
- ForceChargingOff
- ForceDischargingOff
- TurnBalancingOff

* Check if a device instance is already used by creating a PID file

* Log and execute SOC reset to 100% or 0% only once

* Update GitHub workflow and issue templates

* Fixed LLT/JBD BMS with only on temperature sensor #791
#971

* Fix warning on reinstall

* Fix missing IO control for JBDBMS #992
#992

* Prepare for removing dev branch

---------

Co-authored-by: ogurevich <[email protected]>
Co-authored-by: Bernd Stahlbock <[email protected]>
Co-authored-by: wollew <[email protected]>
Co-authored-by: Oleg Gurevich <[email protected]>
Co-authored-by: peterohman <[email protected]>
Co-authored-by: Strawder, Paul <[email protected]>
Co-authored-by: Paul Strawder <[email protected]>
Co-authored-by: Samuel Brucksch <[email protected]>
Co-authored-by: Samuel Brucksch <[email protected]>
Co-authored-by: ArendsM <[email protected]>
Co-authored-by: Meik Arends <[email protected]>
Co-authored-by: Marvo2011 <[email protected]>
Co-authored-by: cflenker <[email protected]>
Co-authored-by: cflenker <[email protected]>
Co-authored-by: Cupertino Miranda <[email protected]>
Co-authored-by: Martin Polehla <[email protected]>
@p0l0us
Copy link
Contributor Author

p0l0us commented Mar 17, 2024

I found the CAN_FRAMES are different for Black and Silver JK Bms. So I introduced another fix to deal with it: mr-manuel#24

image
image

Sign up for free to join this conversation on GitHub. Already have an account? Sign in to comment
Labels
bug Something isn't working
Projects
None yet
Development

No branches or pull requests

2 participants